Hello All,
I?m new to this forum. I?ve been lurking here for a long time but I decided to join now so I could post.
I love the sound of tape. I have three Technics RS-1500 tape machines. They are all stock and in working order. The third machine I bought didn?t function properly at first. I bought it with the intent of using it to learn how to repair and adjust these machines. And if I couldn?t fix it then it would become a parts donor machine to support the other two. I also have about 400 vintage commercially pre-recorded R2R tapes that I'm slowly playing my way through.
Well I ended up fixing it so now I have three fully functioning machines. Then Charles King suggested I document my repair experience on this forum. He and I met at a NNETG meeting; Thank you Charles. Maybe this post could be part of an ongoing thread that would be a repository or diary of problems and solutions to debugging and repairing the RS-1500 machines right down to the component level. Perhaps similar threads could contain this information for other brands.
Over time as problems arise with the machines I own I would add that repair experience here and maybe others could do likewise.
I have a background in electronics. I?ve been working as an electrical engineer since 1982 with a heavy concentration in analog circuit design including CMOS integrated circuit analog design. I?ve been a long time student of audio electronics although I?m not much of a do-it-yourself type since I get my fill of electronics at the day job.
Although I?m not a Tape Project subscriber I?m glad new master quality reel to reel tapes are being made available. I think this helps to keep the format alive. I hope the business continues to be successful.
I welcome your comments and suggestions on the content, level of detail, errors and so on.
The following assumes that you have a service manual with schematics.
OK, so here it goes:
Technics RS-1500 Repair Diary:
Symptom: Machine went into rewind mode immediately after power up and none of the turbo touch keys responded.
Solution: Replaced TR817. This transistor was not switching as intended.
Result: The deck powers up in the correct state and all controls respond normally.
Symptom: Blown PCB pad at the ground lead of C807 in the supply reel motor torque control. I discovered this by visual inspection. This must have happened while I was repairing the control problem.
Solution: Removed C807 and repaired the missing pad with a small piece of copper tape and solder. Replaced C807 in the supply reel circuit and the corresponding C808 in the take-up reel circuit as a precaution.
Result: The Torque Control sawtooth ramp looks normal on the oscilloscope.
Symptom: Take-up tension arm oscillated up and down every once-around of the take-up reel in playback mode.
Solution: Replaced pre-driver transistor TR732. It had low current gain (beta). Also replaced pre-driver transistor TR734. It had completely failed and wasn?t driving the base terminal of the motor driver power transistor TR740.
This did not fix the tension arm oscillation but now all motor control and driver waveforms are pro forma.
Next I checked if the motor had a ?flat spot? where the friction of rotation increased at any point in its rotation. And sure enough it did. A subtle change in torque could be felt that occurred once per revolution. I did this experiment with the motor removed from the machine in anticipation of having to repair it and also so it could spin free of the brakes.
To inspect and lubricate the take-up reel motor shaft I remove the three screws at the rear of the motor. There are three layers held on by those three screws, the rear plate, a black spring plate and a plastic thrust plate. I kept these together and in the same order after I remove them. I didn?t touch the reel table height adjustment screw and thereby avoided having to readjust it later.
A c-clip is now exposed that prevents the motor shaft from being pulled out of the motor when changing reels. Once that and the washer behind it were removed the shaft pulled out easily by pulling hard enough to overcome the magnetic force.
Visual inspection of the shaft and sleeve bearings turned up nothing obvious. I applied a small amount of turbine oil (Zoom Spout) on the shaft, reinserted it, spun the rotor to work the lube in and tested for smooth rotation by hand. I did this process several times until I could no longer detect any torque variation. Once satisfied I reassembled the motor and installed it back into the deck.
Result: The take-up tension arm remains steady in playback mode. The machine is now fully functional and sounds great.